Southern Pacific 9010

Mechanical Work
Page 6


-- Update October 21, 2018 --

And it came to pass that the handbrake mechanism was finished and installed.  Bill's craftsmanship coupled with an original brake wheel from Germany and a lovely new label from Bob Zenk make quite a sight.

The last time we had the engine running, we noticed that the exhaust was spitting oil droplets.  Bill and I ran a compression test on the engine and found the cylinders reasonably equal except for number 15 which was around 150 psi less than the others.  Rob Fern had arrived for his annual working visit so we decided to remove the turbochargers and see if we could find where the oil was coming from.  Upon removing the rear turbo, we found the exhaust outlets from cylinders 9 and 12 to be oily and under the front turbo, number 10 was oily with number 7 just starting to show wetness.  This was bad enough but upon inspection of the turbos, we found that the compressor section of the front turbo is soaked with oil.  I decided that it should not be run as the oil from the exhaust was making a mess and it is likely that the problem would just get worse.  We will be rebuilding the engine in the near future because of leaking cylinder liner seals so while the oil situation is a setback, it means that we can concentrate on the cosmetic part of the restoration.  We have proved that the transmission is in good working order and the truck gear boxes run quietly.

-- Update May 19, 2019 --
In preparation for removing the engine, we had to build a stand on which to mount the 15,000 pound lump.  In reality, it would only weigh about 13,000 pounds due to the removal of the two turbos and the two aftercoolers.    With advice from our friends in the United Kingdom, the
Western Locomotive Assoc. and the Diesel Electric Preservation Group who have expertise in Maybach engines and diesel hydraulic locomotives, we designed the stand using mostly available scrap materials.  It is mounted on a pair of flanged wheeled axles rescued from a piece of maintenance-of-way equipment.  Once it was finished, Dee provided it with a good cleaning and a coat of zinc oxide paint.

Before removing the engine, we once again removed the turbochargers and bolted them to stands that Dennis made.  My grandson Matthew is taking a look at the top bearing area of the front turbo.  This is the one that is pumping oil into the intake system, an issue that will have to be rectified.

Another thing removed was the exhaust outlet assembly.  It has a "pan" around it that is supposed to catch rain water coming through the exhaust stack hole in the hood.  There originally was a hose or pipe that drained the pan but it was long gone.  The pan itself is in terrible shape being more rust and luck than actual metal.  A new pan will be fabricated before the stack is reinstalled.

Dennis and I had been spending time disconnecting motor mounts and other connections in preparation for the big lift.  And then came Saturday, May 18.  Ed, owner of Engineered Crane Services arrived promptly at 8am with his lovely 40ton hydraulic crane.  By 8:30, we were ready to do the lift.  After a couple of trial pulls to determine balance, the engine easily came out under the control of Bill's watchful eye.  Ed positioned it so we could bolt the engine mounting angle irons to the block and then Bill and Dennis set it into the stand while Dee and I took photos.   I was glad to see that the removal of the engine did not materially effect the coupler height of the 9010.

While the crane was on site, we re-installed the number 2 engine hood.  This marks the first time since September 30, 2014 that the major bodywork on the 9010 has been complete.

I was relieved to see that once the hood was in place, the lettering lined up properly.

-- Update March 29, 2020 --
On the last day of May, 2019, we received a large crate of parts from MTU.  The crate contains piston rings, gaskets, rubber parts and some very special tools.  This was not all the parts we would require for the rebuild but we will not know what else we need until the engine is disassembled and we could see what was worn out or defective.
Shortly after the engine was relocated to the shop floor, we began its disassembly.  Rob started removing the exhaust elbows.  These connect each head's exhaust port to the turbochargers through connections in the bottom of the turbos.  There are only 12 of these as 4 heads on each side share elbows.   Dee soon went to work bead blasting them.


We removed the oil pan in order to eventually get at the connecting rod bolts.  There are about 100 small studs holding the pan onto the bock.  This was our first view of the underside of the engine.  Within a few days, Dee had cleaned the inside of the pan.

Back on top, work started to remove the cam boxes.  They are very heavy and are held down to the heads with over 40 bolts.  A special fixture had to be fabricated in order to hold the assembly at a 30 degree angle.

With the cam boxes removed, we had access to the head bolts which are serrated and require a special tool from MTU.

Once the heads started coming off, we had our first view of the tops (crowns) of the pistons.  The one in the second photo shows the results of a worn out furnace.

Each cylinder head has a "furnace".  Initial combustion does not take place within the cylinder but rather in an area above the furnace.  The flame then travels out of holes in the furnace and propagates over the top of the piston.  The furnaces are made of a chrome-moly steel that is very hard, but over heating can cause its flame ports to wear.  Once worn, combustion becomes inefficient which leads to problems like knocking, smoking and general loss of power.  Photo #1 illustrates a good furnace while the others in this set show some of the 6 worn burners we found on this engine.  Evidently, overheating was a chronic problem.

Bill fabricated a complete set of burner removal tools thanks to some parts sent from the UK by one of our team but we were unable to remove any of the worn burners.  

We also discovered that several cylinders had suffered from water seeping in through the exhaust valves.  The valves and valve seats on this head are destroyed as is the surface of the piston crown.  Both the head and the crown will have to be replaced.  I had resisted the idea of taking any parts from the #1 engine but the condition of this head and the need for burners convinced us otherwise.

According the service records, the 9010 was put out of service because of a failure in the number 9 cylinder of #1 engine.  There is no record of what the failure actually was.  The left bank of #1 was taken apart so that the #9 head could be removed but was then simply thrown back together leaving most of the bolts and all of the injectors in the trash bin. We know that we needed 7 heads for the good engine (6 because of bad burners and 1 because of water damage).  When we removed the heads from the left bank of #1 engine, amazingly we found that we had all 8 heads with good burners but head #9 looked suspicious.  Photo #2 is the crown of piston #9.  Note that it has two missing crown bolt caps and one broken bolt.  Note also that it is extremely clean with no sign of carbon at all.  This made me wonder if there was not a crack in the cylinder head and thus caused us to reject this head for reuse.  While in that engine, I removed 4 crowns as we had several bad ones on engine #1.  One crown gave us quie a surprise with a completely shattered top compression ring.  

Next to come out of engine #2 were the pistons and rods.  This engine has what are called "fork and blade" rods.  Most internal combustion engines have the connecting rod bearings sitting side by side on the crankshaft journals.  This requires that the cylinders be slightly staggered and thus increases the overall length of the engine block.  Fork and blade engines like the Maybach (and EMD's) use a different system whereby the rods from opposing banks connect to the crankshaft in the same space.  Photos #1 shows the two rods in place on a common crankshaft journal.  Photo #2 is of a blade rod and photo #3 is of a fork rod.  The blade rod mounts within the open space in the fork rod and thus makes for a more compact engine block.  Eventually, they were all removed and stored on a specially built rack.

The top of the piston is called the "crown" and on this engine is removable.  The crown contains all of the compression rings while the oil control rings are mounted on the piston, one above and one below the pin.  The crown is attached to the top of the piston with serrated bolts which are in turn covered by caps.  Of course, both the caps and the crown bolts require special tools.  Removal of the crown reveals the crown oil cooling passages.  The small tube seen at the top of photo #3 is the top end of the tube in which the cooling pipe rides.  The lower part of the cooling pipe is shown in photos #4 and #5.

Having the pistons out of the cylinders means that we could see the condition of the liners.  Ultimately, we found 5 liners that had sufficient problems to make their replacement necessary.  The one seen in photo #1 shows the result of having water standing above the piston for a very long time.  The liner in photo #2 belongs to the cylinder head and piston crown shown above.  Notice the two long deep scratch marks in the liner.  They were caused by the piston pin being loose and digging into the liner wall.  One of the two snap rings that hold the pin in the piston was missing.  This liner also exhibits the corrosion caused by water standing in the cylinder. 

Dealing with the heads took nearly 2 months.  All valves were removed (using our custom valve spring compressor), the heads cleaned and tapped holes cleaned out.  All valves and seats were hand lapped. 

 The 7 rejected heads were all put back on engine #1 and that side of the block was closed up.

The next order of business was the removal of all of the liners.  This was necessary because we knew that some of them were defective and all of them had 50 year old lower seals.  The liners are pushed into the block and we knew that they would not be easy to remove so we built a pulling rig that is powered by a 25 ton hydraulic jack.   By multiplying the area of the jacks piston and the hydraulic pressure applied to it, we determined that it required 24,000 pounds of force to knock the liner loose.  Photo #5 is of the lower liner seal area with the old seals still in place and photo #6 shows 3 cleaned liners.  It was interesting to see the differences between the liners in the same engine. 

As soon as all of the liners were out, volunteer Karl Swartz set to work cleaning the sealing surfaces where the liners seat into the block.  At the same time, we cleaned the top of the block and the mating surfaces for the liners and made sure that the weep holes were open.  We also made cardboard covers for each of the open bores on which we could keep notes on bore work.  The green pieces of tape seen in the photos are to protect the water and oil passenges which were also cleaned.

Early in March 2020, we received our second order of parts which included the 5 new liners and gaskets that we had not ordered the first time.  Now, things can get really serious.

Now that we had all 16 liners available, we started to install them.  The 11 old liners were reinstalled in their original holes but were rotated 45 degrees per advice from our friends in the UK.  All liners received fresh lower liner seals (the orange bands in the first photo) and were sealed at the top with a high quality copper infused silicone.  Hopefully, they will all pass the water test that will come later.

With the liners in place, I could install and align the piston crown cooling (banjo) lines that were removed in order to clean the lower liner seal areas.  There is a very expensive tool available for this one time operation but we came up with our own method.  We took a piston without its oil rings and crown, dropped it into the bore until the rod bearing sat on the journal.  This aligned the piston to the crankshaft.  While the piston was being lowered into the bore, a rod was inserted in the cooling pipe.  The rod has a smaller diameter on its bottom end which is inserted into the cooling line and aligns it to the pipe in the piston.  The crankshaft was then rotated 90 degrees to bring the piston down just far enough to use a small alignment tool that volunteer machinist-bodyman Bill Stimmerman made.  The tool goes around the line and up into the pipe thus fixing the line in place.  At that point, the mounting bolts for the line were tightened so the line could not move.  The piston was removed and the line's mounting bolts firmly tightened.  The whole process was a bit cumbersome but gave us the result we wanted.


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