Southern
Pacific
9010
Operations

Jim Evans Photo
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The
Ground Relay
I got
"separated" (by the SP) about two weeks
after the first K-M hood units showed up in Roseville. I did
get
to hostle the 9004 from the "launching pad" at Roseville to the ready
tracks. My favorite story came after the SP gave up on the
K-M's.
I'm not sure if it was told in retrospective, or maybe was
told
of one of the ALCo's that lasted a while longer. A Western
man,
R.J. Kelly, gets called for an Oakland-bound TBX from Bayshore.
A
long while after he's on duty, the Bayshore roundhouse foreman becomes
aware that he's still sitting on the track that was usually reserved
for #374's power. The RH foreman calls Kelly about why he's
not
moving. "I can't get the Ground Relay to reset."
You
shouldn't have to think about that one for long.
Anyone
need an explanation, let me know.
Tom
Irion
2008
Workin'
On
The "Krauts"
I have a
few stories of working on the "Krauts". They were interesting
beasts. Not everyone liked them. I always suspected
the
shop guys hated them.
The best one was coming west on the Cal-P in 1964 with the 9021 (ed: a
cab unit). Somewhere between Davis and Suisun, everything
goes to
hell. The air goes into full service. The power
dies.
The bells, lights, etc.
We look at each other and go, "What the Hell?".
I go back to see what blew up, to find the face plate of the engine
room control panel on the deck. It had fallen off and cut all
the
switches off!! These were pretty much like light switches; up
was
"on" and down was "off". The face plate, when it came off,
tripped all these to "off".
So I take the plate and put it aside. Turn everything on and
restart the unit. By this time we are stopped. Went
back to
the head-end and told the runner what had happened. Seems as
though the West Oakland shop guys tried to "repair" the face plate's
missing screws with stock US thread screws, which did not work on
Metric. DUH?
A couple of weeks later, while BS-ing with a fireman off the Sacto Div.
the subject came up. He told me that he "fixed it".
He
picked up the face plate, after it had fallen off, AGAIN! and threw it
in a hay field!!! Yep. THAT "fixed it".
In 1963 I caught the "beets" out of Tracy for Union City. My
engineer was J.R. McHale. So we have these 3-4 "Black Widows"
and
to K-Ms (Carbodies) for helpers, on the point. B.
"Smokey"
Weslar was the helper runner. We are slogging it out up
Altamont,
on our hands and knees at Midway, and Mac is pissing and moaning about
how the krauts are junk with no power. I told him they had
had
lots of power. . . if you would run them at full throttle.
(Remember, the K-Ms had a 16-position throttle vs. the US built stuff
at
8.)
Mac says "What makes you think Weslear isn't running wide open?".
"Well, if you look in the cab at the tach on the back wall (of the
trailing helper) it is only about 3/4 of the way up the
scale".
Mac goes ballistic and calls Smokey on the radio to tell him "stop
dogging it!" Guess what? The tach needle goes right
up to
the top end.
That same trip, the beets out of Tracy, we put the power on the head
end and the helper couples up. During the air test, a hose
between the K-<s and Black Widows blew out. Well,
O.K.
We are in the yard and so what's the big deal? The shop guys
should come over and replace the B.O. hose, right? Well, not
right away.
Now. You know this, and I know this. But the K-M
tech that
was there at the time had a blue fit. he could not get it in
his
head why the engine crew could not just take a hose (which all the
units had in their "pieces-parts" bins) and FIX IT!
Guess
what, "Gunter", this is America, not Germany. So after about
an
hour, the show gets back on the road.
This same day (seems like Tracy was a "hot bed" for K-M stories) I got
to chatting with "Gunter". (No. I don't recall the
KM
factory guy's real name. "Gunter" just sounds good.
Who
knows.) During this conversation I was trying to get anything
I
could out of him on how the beasts
worked. He said
two things: 1.) When the bells go off and the lights come on
. .
. it's too late.
2.) He told me, "I have no idea why your railroad is buying these
locomotives. America builds the finest diesel-electric
locomotives in the world.
You call them Geeps".
When the K-Ms first came to the SP, 9000-9002, they were universally
hated. They had some kind of funky reverser thing that took,
like
a couple of minutes to work. I am not sure what got done to
them
to make them "normal" as compared to any other diesel, but it did get
gone. I will say one thing about them, their cabs were
QUIET! Almost too much so. I sort of liked them . .
.
except for the 9021 and the crap face plate.
McHale was the one who made the remark "Did anyone ever think about the
Cardan shaft that was inches under our feet at "X" rpm's and only 3/4"
of plywood between you and it??? Hmmm?"
One more K-M story. Christmas day. After the
dispatcher
finally gets around to send crews west out of Tracy to West Oakland,
about midnight, I get two K-Ms with Dick Bragg as my hoghead.
We were all pissed that "God" (read "Dispatcher") had held us on HAHT
(Held Away from Home Terminal) so long and we were not going to get
home at a decent hour for Christmas with our families. The
conductor was Cy Holcomb (lived about four blocks from me in American
Canyon/Napa Junction). We had a green head
brakeman. It was
cold, foggy and dark. At Pittsburgh, we had a setout that had
to
go in "Gum 1" and double to "Gum 2".
We made the cut on the main. Shoved Gum 1. Cut off
and
pulled to set over into Gum 2. As we were pulling out of Gum
1,
the units started to bog down. More power.
Sand. More
power. Dick says, "I thought these things had
power?". I
said, "They do." Dick says, "Well, they don't . . .".
POW! The air goes in.
NOT GOOD.
So I go back and in the gloom of the fog there are three high-cube chip
cars "sort of on their sides".
NOT GOOD.
The deal was that the new brakeman did not know how to read the high
switch stand target that was the joint track for the Santa Fe and the
SP yard. He split the switch and then we pulled back through
it. (Those chip cars never look good with 110-pound rail up
through their ends.)
I will say this: those two K-Ms buckled down and pulled those
cars through a bunch of rail, ties and ballast.
Yes, Dick. They DO have power!
Dan Ranger 2008
They Were Fast
The only things I can remember about the KM's were that they were fast
- very fast compared to a diesel-electric, and that I could never find
the water gauge to determine if we had ample water in the
radiators.
The trip to Oakland with the 9010 was at night, but the trip from Tracy
to Bayshore was during a beautiful morning. It was too bad
that
someone did not "shoot" us as we climbed the Altamont with a short
train.
Southern
Pacific (and
the Rio Grande) had a dual interest in buying the
KM's. Both railroads wanted EMD to develop higher horsepower
units.
From what I have heard, EMD was happy to stay with the 567 prime
mover. The first order for the 4000 horsepower KM units did
not
not
impress EMD, but when the SP put in the second order, they took note
resulting in the SD-40 and SD-45, and as you know, the SP was the
biggest buyer of the SD-45.
While the
SP wanted
bigger units, I think they also hoped that the KM's
would work out. I can't think that they expected those units
to
be at
the scrappers in but four or five years. Sure glad we used
the
9120 on
that trip in 1967.
C.G.
Heimerdinger Jr. 2008
The Last Trip That German
Engine Ever Made
It
was after April sometime in 1968 because I had been a switchman and I
was called back as a fireman for a vegetable empty reefer drag from
Roseville out of Oakland to Salinas. The engineer was Augie
Carilla and the only reason I remember the trip at all is because of
what happened. We had a German engine with I believe it was a
F-unit trailing and we changed crews at 10th street in
Oakland.
The inbound engineer told us that there was something wrong with the
lead truck on the German engine because every time he went over a
trailing point switch on his side, the engine jumped around
real
heavily. So Augie asked the engineer if he thought the engine
should be changed there in Oakland and the engineer said, "No, we made
it down from Roseville".
So, Augie and I took the train
and being as it is slow all the way out to Elmhurst, we didn't make
very good speed but once we cleared Mulford and got rolling, the first
switch that we went through with a trailing point on his side, the
engine jumped violently and then settled right down. So, he slowed way
down and pulled out past Mount Eden where there was a lot of open track
with no crossings and we stopped and cut the engine off and he got down
while I ran the engine ahead real slow while he walked and checked the
wheels on the lead truck. He couldn't see anything wrong at
all
so we tied the train back together and we went on to San Jose but at a
reduced speed but still, every time we went over one of those switches,
it would bounce around but not nearly as bad. We put out a
note
at Newark to have the engine changed at San Jose which they probably
would have done anyway.
When we got to San Jose, they
headed us in on number 33 track which was the longest track in the yard
by the fence at FMC and when we got down to the end, they cut us off
and we went to the roundhouse. To go to the roundhouse, you
had
to pull down the Santa Clara lead right next to the College Park Tower
and go over a crossover switch and then back through onto the
roundhouse lead. As we were backing through, we got to the
second
switch in the crossover and the engine derailed and went on the
ground. So, they sent us up to go eat and get our rest while
they
rerailed the engine. When we came back after about 5 hours,
they
still hadn't got the engine back on the rail but they found out that
the center axle had broken on the engineer's side right where it was
pressed into the wheel. When it dropped on the ground, it got
cocked and got wedged between the point guard and the truck
frame. We assumed that this was probably the last trip that
German engine ever made.
Errol B. Ohman 2008
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